Green Arrow - What did happen then?
Posted: Sat Jan 28, 2006 2:26 pm
Whilst in the museum today with Flu (passing it around) I listened to the workshop roundup (and nearly colapsed)
So what happened to Green Arrow then, and what's the future?
Scotsman was down, and Green Arrow worked the Tuesday runs fine, and wednesday it went up fine, and was heading back mid Wednesday afternoon, at about 60mph with a 12 coach load (in 1944 a V2 pulled the record, 24 coaches full of solders from Kings Cross) when it was somewhere around Malton and there was an almight crack and steam came out of every where.
The engineer was on the train, and had a look.
The middle cylinder had sheared off at the axle, and fallen down on to the axlethe foward motion then drove it back forward and pushed it right through the front causing the major damage. The engineer has a look, they manage to get it clear and he said to carry on back on 2 cylinders, and it was only 40 mins late getting back!
The middle wheels ( with a huge gouge in the axle) have gone away to be tested with the lasers, and aren't buckled, they're fine.
The cylinder they have is slightly narrower, but should do the job. Some of the bits are in, and they made a wooden jig to drill the holes.
When the wheels get back, it should (all being well) running to Scarborough this Summer.
The Super D that's in, is being paid for by Pete Waterman, (although the museum owns it) and it almost done, but there is the slight problem of getting it in to the middle track to drop the wheels back in.
So what happened to Green Arrow then, and what's the future?
Scotsman was down, and Green Arrow worked the Tuesday runs fine, and wednesday it went up fine, and was heading back mid Wednesday afternoon, at about 60mph with a 12 coach load (in 1944 a V2 pulled the record, 24 coaches full of solders from Kings Cross) when it was somewhere around Malton and there was an almight crack and steam came out of every where.
The engineer was on the train, and had a look.
The middle cylinder had sheared off at the axle, and fallen down on to the axlethe foward motion then drove it back forward and pushed it right through the front causing the major damage. The engineer has a look, they manage to get it clear and he said to carry on back on 2 cylinders, and it was only 40 mins late getting back!
The middle wheels ( with a huge gouge in the axle) have gone away to be tested with the lasers, and aren't buckled, they're fine.
The cylinder they have is slightly narrower, but should do the job. Some of the bits are in, and they made a wooden jig to drill the holes.
When the wheels get back, it should (all being well) running to Scarborough this Summer.
The Super D that's in, is being paid for by Pete Waterman, (although the museum owns it) and it almost done, but there is the slight problem of getting it in to the middle track to drop the wheels back in.